NStiesi's Projects

I’ve been using a manual air blast, and I have tried trochoidal as well. I couldn’t quite get to full depth. I think some of my issue was how thin the material was, meaning it heated up quick. Also my tools have alot of aluminum build up that I could t really see until I took them to work and looked under 30x power microscope

I have some single flute mills coming in the mail today.

This is my biggest cut yet, based on size and run-time…Its a card game board for my son as a bday present. There will be a second side, which gets connected to this one with a hinge to fold up when not in use. It will definitely get some stain and tung oil, and i am considering coloring the character and the logo with paint. Its not perfect, some of the round pockets are oblonged due to having to re-mount the part and enlarge the features. Even with a hard origin on the table, the board was skewed slightly, and the error projected across 22". Side 2 ought to go smoother with lessons learned.

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That looks great. I am sure some finish will bring out a lot more contrast. If you do end up painting, unfinished wood can soak it up in the fibers. Which will look like it bleeds a bit. There have been some discussions here about it. I would definitely put whatever stain and finish on first and then try the paint, so the wood will soak less up. I don’t know the different finishes well enough to know if tung oil is strong enough to keep the paint off the wood. Might be worth it to so a quick test in a piece of scrap.

Thanks for the advice, Jeff, i will keep that in mind.

Side 2 went perfectly, all kinks sorted out. Just a little chatter in the deeper pockets during full depth adaptive clearing; i was taking a big bite i guess, even for pine. That and my machine is not cutting square. At this point, not really sure if the hard origin is out of square to the machine, or the X Y rails are out of square to eachother…maybe a little of both.

On this job, I did not cut all 4 sides. I laid 1x12" stock up to the hard stops on my table (an aluminum “L” bolted to the table), then just cut the board to length with a slotting toolpath. Even if the XY were perfect, if the board was askew to the machine I would get a slight trapezoid.

I do not have dual endstops (which in hindsight, I should have done). I use a VERY beefy machinist square on the rails during my power on procedure. I actually lay the square on a 2x4 to raise it up, then clamp the x and y rails to the square before powering on the motors. This seems to get me close.

These boards are also 22" long, so my error is projected, and my machine is 2’ x 4’ (I would hate to see the error over a 4 foot cut!). I am probably in lowrider territory, I knew that when I started, but I resolved to live with the shortcomings. Luckily for this project perfect square is not critical. Since the two sides are both out in the same direction, they will fold up flush to eachother and no one will be the wiser!

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Oh yeah…that’s the stuff. I love it when a plan comes together!

Tomorrow we poly. Then assemble. Delivery to the “customer” is Saturday!

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The card table is done, will get some pictures tomorrow after party time.

Switching gears, this was supposed to be an anniversary gift back in may, but got put on the back burner. Apparently 10 years is the aluminum anniversary

After some sanding, filing, scotch brite, and polish:

I’d like to polish it more. The job itself went ok. My machine is big and chatters a lot on heavy cuts. I also burnt up one end mill going too aggressive with an adaptive clear. 10% stepover at .25 doc was too much, had to cut it in half then everything was pretty happy.

Slotting was done at .015 doc, 450mm/min, machine was very happy here.

Finally I have to plane my table someday; had some inconsistencies in the roundover cut.

I plan to mount this on a nice piece of oak, stain and poly

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Final product:

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Solid projects! Thanks for sharing.

My first test of an inlay. The base was plywood, and I sanded through the veneer inadvertently. This was made out of scrap just for process development purposes.

The fit was ok, even though I made some mistakes. I need to make deeper bevels next time, and mind the radii on interior corners. Enough glue and clamping covered up some fit issues.

All in all, it’s a solid process that I can expand on, so I’m happy!

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I don’t think anyone could complain about that fit, good job.

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Thanks! That means something coming from “the maker” lol. It’s amazing that (and I mean NO offense) that “pipes and plastic” can achieve this level of accuracy. Speaking of which…

Aluminum and I are coming to an understanding. This was cut with a 2mm single flute, from 1/8" hardware store architectural “bubble gum” aluminum.

I predrilled with the cnc, then finish drilled and tapped by hand. For the bearing, it took me a few tries, but I found that a line to line fit was perfect, but I had to do 4 finish passes to get the size right: 1 removing .005" then three zero thickness passes to clean up and account for deflection. Once I did that the light press was perfect. This is another part for the model engine project.

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Pistons, crank plate, connecting rods, solenoids installed in 3d printed housing and backplate. Once I prove this out I will make the housing and backplate from aluminum (not sure how yet, housing is too big for mpcnc).

The solenoid flanges, rods, and crank plate are all mpcnc contributions. Rest is manual lathe and mill work.

The mpcnc will be put to work cutting counterweights, hopefully tonight.

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Time to think about minimal mist cooling… Look at what Sebastian End offers in Germany

A post was split to a new topic: NStiesi’s Projects - PCB

You can also do air blast if mist coolant looks too messy.

After taking some time off and working on other projects, iv been running the mpcnc a ton in the past week. Couple jobs for work, some for my zenxy coffee table, and a few gifts for people. This one came off today. Nailed it ony second try:

Just plain ole pine. I needed something that was available and took stain well. I’m gonna attempt to fill the carvings with colored resin.

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First pour done. Color mixing with dry pigments seems to be a bit of a crapshoot, but perhaps I’ll get better at it. I measured, but with the low volume of resin I was afraid of affecting the cure by putting in too much. Otherwise, im happy so far! Machining time was about 1hr and 4 tool changes for each side. End product will be a rack for mouse ears.

I’m also going to stain the wood dark so the contrast will be improved. 3 days of curing before I can sand and think about all that.

This was also a bit of resin practice before doing the soccer sign…which is more practice before pouring for my ZenXY table!

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Getting there. A bit disappointed that I didn’t add the pigment slower, the pink came out darker than desired. Should have mixed in some white…ugh

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Did a fishtank lid for my brother from 1/2 polycarbonate.



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